So the first test is to try using a 12v drill motor to drive the center leg lift. It’s pretty torquey and I’ve geared it down. I’ll drive using a DC driver and Arduino (dedicated Arduino for the 2-3-2). Let’s see how it goes. Still printing the mounting frames.
Michael Baddeley
2018-07-15 12:18:49 +0000 UTCRay Edgley
2018-07-15 11:41:49 +0000 UTC